Page 7 - MESCO Newsline 11th Edition
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---MESCO Newsline

                REVAMPING OF 30 MW CAPTIVE POWER PLANT

                                            MESCO STEEL - II

                                                            The main objective behind the two
                T 'he CPP we have is of 30 MW capacity & comprises   to reduce the Steam & Power Cost
                                                             major initiatives taken this year was
                  of 3 Nos of Boilers i.e. 1 X 60 TPH coal & dolo-char
               fired CVL Make Boiler and 2 X 34 TPH Waste Heat   by utilizing & maximizing char (%) in
               Recovery Boilers with a total installed capacity of 128   our AFBC Boiler and to enhance
               MT/Hr steam generation and operating capacity of   capacity utilization of our Turbo
               Max 110 TPH (As both WHRB steam generation is   Generator by reducing the vibration   V. N. Tiwari
                                                                                              GM CPP &
               depends upon the 2 Nos DRI plant process operating   level at its low speed end to   Factory Manager
               condition) to generate 30MW power with lx30MW   minimize our energy import bill.  MESCO Steel - II
               Siemens make STG set.                                                           Jajpur

                                         AFBC Boiler Sparger Hopper Bed Modification - (Cost Comparison and Payback Analysis (5) 60 TPH Stem Output)
                                          SR NO     KEY PARAMETER      BEFORE      AFTER       REMARKS
                                           01  AFBC Fluidized Bed  Distributor Plate Bed  Sparger Flopper  D.B Plate-CVL make
                                                                   svstem with Wind Box Bed Svstem  Sparger Hopper-Thermax
                                           02  Char Utilization capability on  30%  60%   By Weight
                                               continuous basis
                                           03  Average Coal Consumption per  270MT-280MT  210MT-220MT
                                               dayatl00%MCR
                                           04  Approx. Coal Saving/day @330   Approx. 50 MT/Day  Approx. 50 MT/day @
                                               days                                       1500MT/Month
                                           05  Estimated Annualized Coal                  Approx. 4.7 Crore
                                               Saving @Rs.2900/MT
                                           06  Cost of Project (Thermax & In-             Approx. 3.5 Crore
                                               house)
                                           07  Pay Back                                   < 09 Months
                                                                   mUJ
                                               Pictorial Viewof AFBC Bed system
                     New PA System
                TG SET MAJOR OVERHAULINGH - fCost Comparison and Pay back Analysis @ 20 MW GENERATION)
                 SR NO  KEY PARAMETER     BEFORE    AFTER     REMARKS
                  01  Specific SteamConsumption  5.0MT/MW  4.10 MT/MW  Include all Auxiliary
                  02  Low speed side vibration Level at 160 Microns  60-70 Micron  Consumption Replacement of all
                      TG Low speed Gear-box End               Bearing, Base Grouting and post
                                                              alignment
                  03  Vibration Level at Alternator end  190-200  125-130 Micron  Replacement of all Bearing,
                                          Microns             alignment& in-situ Balancing
                  04  Maximum Loading Limit  22.0 MW  >24 MW  Due to significance reduction on
                                                             Vibration at Low speed end &
                                                             Alternator
                  05  Estimated Annualized Saving @  Approx.- 4.3 Crore  Considering 300 days of all 03
                      Rs.3.0/Kwh                              Boiler Availability & Steam From
                                                              Process Boiler >40 MT/Hr
                  06  Cost of Project (SIEMENS &  Approx.- 2.5 Crore
                      Inhouse)
                  07  Pay Back            < 07 Months
               The above initiatives were taken by the management are likely to provide immediate boost towards the profitability of the
                organization.
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